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I'm trying to incorporate a drop-in nozzle, but interchanging them will be a fair amount of dissasembling. One major disadvantage is that sold comercially, Radius would have to be shipped fully assembled, and would be judged as extremely heavy, and bulky. |
I just ran across this thread today and I am BLOWN away. This is some very cool custom work.
I'm embarrassed at my setup now. I've been using a 350gph pond pump in a 5 cubic foot freezer with a mixture of glycol/water through a Z4 waterblock. Condensation is a pain, but it does the job. I'm amazed at where you have taken this project. Good luck bro and keep on going.:D |
Rattlehead thanks for the compliment.
little update. and i spent 3 hours sunday morning soldering the block up.but now block is together.monday i let acid set in the block to clean it some after the solder and heat got to it....now i have finish machined it and currently being pressurized for leaks.280 psi for a day or two i hope will do it.so with a little luck this weekend i can get the chiller cranked up and see if it works. block being tested.http://members.fortunecity.com/ajr01...ze.of.Clip.jpg |
well a little weekend update.i got the cooling unit up and running.am running now and testing for leaks.i hope to get my load bench finished so i can start loading and testing the unit under stress.i used some r12 just to give it a fill and test with.my chiller tank seams to be doing good.i checked it and seams to be flowing real well at -27c with no signs of thickening up.evap temp was running well under -40c .not too bad just breaking it in.
http://members.fortunecity.com/ajr011/complete.jpg |
Dang, that line isn't just cold, it's cold all the way down the pipe! That's going to be one cold CPU!
What do you have planned for anti condensation? |
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Simply amazing work. Great job, man! Wish I had the knowledge, tools, technical skills, ballz, and sheer audacity to attempt something like that :)
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Bowman, I plan on attempting a similar project over my christmas holidays. I already have a few questions and I was wondering if I could pick your brain about them. Can I e-mail you sometime?
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well a little weekend undate.been running unit on and off all week.well today (sunday) i set out to try and load up the unit with a 156watt pelt on the evap and 80watt pelt on the chiller.well middle of the week i changed the capillary tubbing and made it longer to help bring down the temps while i was using r502.seams i set the unit up for r22 capillary and r502 flowed too easy,more than i expected.making the evaperator flood with excesive refridgerant.this makes the temps rise slightly.best it would get is about -44f on the evap.but because i am running dual capillary tubes one feeding the evaperator and one feeding the chiller..it is very hard to get the best of both the chiller and evaperator block temps.get one good and hurts the other,,so i have comprimised to come up with a nice in the middle setup.i lenghened the evaperaor block capillary tube to 120" od .036id tubbing. and set the chiller to 90" of .031"id tubbing.now this hurt by load temps with a 156watt pelt.evap block cannt keep up with the heat load.rises to about 32f(0.c).but then again no cpu will put out that kind of heat.but the chill did very well with a 80watt pelt on load.keep temps around 24f (-4c)in the coolant after a couple of hours of running.
overall the cooler is working pretty good.got a no load temp of -52f (-46.6) on the evaperator cpu block and a -11F (-23.8c) in the chiller tank.chiller is taking 2 hours to reach -12f(-24c) and has a reservoir of 2 gallons. here is a little pic http://members.fortunecity.com/ajr011/52f0f.jpg |
Bowman: earlier in the thread you said that you are going to reduce flow to keep temps on the NB and GPU in line, but won't the reduced flow have a tendency to allow your coolant to get awfully viscous, especially with an 80W load temp of -4C?
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well i am only reducing the flow to the chipset now.i wanted to see how well the chiller could handle a pelt pushing 80 watts,
i am going to water cool the video gpu on my radeon 9700 pro.with the help of a pelt.the cold plate side of the pelt was running about -20f(-29c) that should be more than enough i hope to alow a good overclock on the card.and with that it might warm the coolant up enough to alow me to leave the chipset coolant vavle open without having to reduce the flow to help with the condensation. but time will tell.i am waiting now on my replacement board from abit .at7max2 been on a waiting list for almost 3 weeks now.abit says they are waiting on the newest revision to help with some of the problems they have been having. that and i will be about another couple of weeks untill i get the new aluimiun case for the motherboard and cooler finished or at least till i can get the thing mounted to test in. |
well i got the system better tuned i think.i lost the sub -50 temps on no load but my load temps and chiller rate of drop have made up for it i think.system bottoms out at -38c no load but the load temps with my test peltier have gotten much better -21f (-29 to -30c ) load temps.chiller is now below 0c close to 30 minites time.and 2f (-17c ) in right at a hour.
http://members.fortunecity.com/ajr011/tempchart.jpg http://members.fortunecity.com/ajr011/-3702.jpg |
What did you do? Did you reduce the capillary tube length or increase the amount of refrigerant charge? It sounds like you are getting higher refrigerant flow but also lower suction vacuum (higher pressure at the suction side of the compressor).
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p.s i am working on a mouting system right now also.i have hand made a evaperator block inclosure cell.to hopefully make it easyer to control the condensation easer |
Bowman, please continue your work. This is really great stuff.
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well here the weekend update.i have been working on a mounting system and a better way to insulate from condensation.i have taken a sheet of sheetmetal and formed me a sealed box.this is going to seal against the motherboard and i hope help in stoping condensation.
i thought if i was going first class with the cooler why not do the best i can on everything else. and machined me out a waterblock for the radeon 9700 with a peltiter.i even premachined the cold plate to fit the ati shim. http://members.fortunecity.com/ajr011/coverblock.jpg picture of the evaperator mounting box which i made in 2 halfs to make it easer to mount and remove.and also showing the video block which i hope to start load testing this week on the cooler unit. http://members.fortunecity.com/ajr011/cover.jpg also pic of evaperator box being tested for condensation and how well it will insulate the evap.evap is running at -60f (old cooler i use to test with)and no condesation shown yet |
Bowman>>
How do you make sure that the oil for the compressor returns to the compressor, when you are using Direct Die cooling ? All compressors do use oil right ? |
Yes they all use oil.The oil follows the refrigerant vapor back, so you get a good return of oil.
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well the only place you have a problem at ,will be in the condensor.the evaperator block has refridgerant boiling away so fast it pulls the oil along with it.
now the condensor is where the vapor is compressed and cooled into a liquid.there you can have a problem of oil collecting in low spots if you are not carefull.but unless you have a large area plumbed wrong or used a wrong condensor(such as using a old evaperator as a condensor) you will not have any problems |
sorry guys i had a bad weekend so i didnt post as much.
but have made a few changes and i should be posting some updated pics and test results. but this is one from tue night. i totally removed my fans from the condensor and added 2 more 92 mm fans for a total of 6 therma controlled fans.they are so nice.very quite while running with no heat and slowing increase in speed as the condensor temps rise.cannt see to well in picture.but a little ever night or so.cannt wait until i slide it into my case.waiting on abit on my replacement motherboard. http://members.fortunecity.com/ajr01...f.IM001341.JPG |
GOT INSULATION BEOTCH ? :dome:
I have a question. Have you ever had a problem with those hoses cracking from getting so cold? I'd assume you don't move them while they are that cold anyway, but just out of curiousity. It looks like plain vinyl hose. Mine would get REALLY hard and I'd worry about moving them and having them just shatter on me.:eek: |
SURE I WORRY ABOUT THE COLD BREAKING THEM BUT THE VINYL HOSE IS VERY EASY TO USE I HAVE SOME REINFORCED HOSE BUT IT BECOMES VERY HARD TO WORK WITH INSIDE OF A TIGHT AREA. I HAVE SOME ALL SILICONE HOSE BUT I CANNT SEE INSIDE AS WELL .TO CHECK THE FLOW ONCE IN A WHILE IT IS NICE.
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well trying to keep from posting 2 pictures ...lol what you think.
o well i show both i have done a few more modifications to the unit. one is I found the compressor heat load is very large.compressor would get to over 74c (165f) on the back side where it was getting no air.so as i am planning on siding this into my new tower case.i know it will get hotter if i didnt do something.so i have made a aluminum shroud that will force the air from the condensor to move around the compressor.and i added a small fan to help push it around the back of the compressor....that made a good improvement in my compressor temps.now adveraging about 65c (155f)which i dont worry about. second a also made a aluminum cover for my flow control vavles and made a nice place to put my video gpu coldplate temperture readout. i fully insulated the evaperator this time and removed my load plate .temps dropped so fast i almost lost track.in 45 minutes the chiller (4.5 liters of coolant) dropped from 21.1c (70f) to -25c (-13f) started up the video peltier and coldplate went to -48.0c (-54.4f) while the chiller maintained a temp of -21.6c (-7f) the evaperator for the cpu dropped to -44-4c (-48f) in a record time of under 3 minutes 2 1/2 minutes to be more acurate.but as the refridgerant floods the evaperator the temps will rise because of excess refridgerant.starts to flow like a liquid and boil off much slower.but as soon as a heat load is applied it will come back to life.as i have set the charge for a heat loaded evaperator.i set it with a 80 watt peltier and got it to maintain a temp of -30c with full load. http://members.fortunecity.com/ajr011/charttest.jpg http://members.fortunecity.com/ajr01...test121902.jpg |
Looking really good :D
I can relate wth you and the compressor heat.I haven't monitored the temperature of my compressor, but I am sure it is around 70c or so.Problem with that is I don't have enough capillary, so the heat from the compressor adds to the high side pressure, if the compressor is cold then I don't get any cooling until the system warms up. |
Bowman, I have a question. I have a watercooler, anyhow I'm going to be making a phase change block, somewhat like the one you made. My question is this, the compressor is currently charged with R12. I plan on discharging the system, making the modifications (adding the block etc) and then recharging the system with some new R12 (I have two brand new canisters). I have the oil which is used with R12, but do I have to add some when I recharge the system, or will oil have been added from the factory... or by the watercooling company, since the system had been charged with R12?
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Ok, thanks for the info bowman.
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Bowman, is silver solder strong enough for use on a refrigerant system?
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ok now when you say silver solder that term is when you brase with a special mostly silver brasing rod.that is the strongest off all brasing or solding.it is second only to welding.but no one here is every going to use that stuff.i have some at work but for one is exspensive and very hard to use. i think you are refering to a plumers solder lthat has a silver additive like what i am using.mine is a 95/5 lead free solder with silver added for extra strengh. i am going to give everyone a site to go to.it will show how to properly solder and like it says if done properly the soldered joint will be as strong as the copper pipe you are soldering to.http://www.nci-marketing.com/solder.html and also a picture i have showing the spec of a 95/5 solder and that it will withstand 540 psi at 200f degrees so you wont have a problem if done correct. my entire system is soldered with 95/5 silver based lead free solder napa part #777-1865 http://members.fortunecity.com/ajr011/solder.jpg |
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