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Unread 11-24-2003, 06:39 PM   #201
Sin22
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Interesting that DD is fine with letting so much of the IHS "peak" through on the A64, and yet Swiftech came out with a whole new baseplate to cover the small 2.5mm or less showing on either side. Sort of shows the mentality of both companies to me.I brought this up sometime ago too.
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Unread 11-24-2003, 06:47 PM   #202
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On a somewhat related note, initial reports are that removing the IHS from A64s is a bad idea. Lots of chipped edges so far I hear.
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Unread 11-24-2003, 06:52 PM   #203
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Quote:
Originally posted by pHaestus
On a somewhat related note, initial reports are that removing the IHS from A64s is a bad idea. Lots of chipped edges so far I hear.
Sounds like the good ole AXPs anyhow.

LardArse has had two A64s "naked" and both were fine under his fridge chiller.

Also, leaving teh IHS on and going sub-zero is a bad idea due to the condensation building up inside of the IHS.
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Unread 11-24-2003, 06:53 PM   #204
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Well for people like us the IHS is a bad idea anyway. The comments I read were at xtremesystems.org; not sure what kind of abuse the chips saw there
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Unread 11-24-2003, 06:57 PM   #205
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haha, depending on who it was who actually had the chip. I can think of a few who might be a tad over enthusiastic.

So it seems to be a bit of a predicament, take off the IHS and chip the die. Dont take off the IHS and let condensation form and kill it that way. Life is full of hard choices.
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Unread 11-25-2003, 11:52 AM   #206
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The problem with removing the IHS of the A64's is that whereas they work fine when mounted, the corners start cracking because the pressure of the A64 mounts is greater than the XP system was and it seemed to me that the cores may be more fragile than the smaller XP ones are. Because all of the A64 mounting systems are set up for a very large amount of force as called for by AMD A64 specs, it would be up to the user to figure out how to adapt a custom mounting system to provide less force if the IHS is removed. And from my own testing, I have come to the conclusion that with the right amount of force on the IHS, it can perform as good as removing it in any case.
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Unread 11-25-2003, 12:38 PM   #207
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Quote:
Originally posted by xgman
I have come to the conclusion that with the right amount of force on the IHS, it can perform as good as removing it in any case.
Somehow I highly doubt that. Maybe, maybe when using phase change the differences would be minimal but from my experience with the P4, removing the IHS improved temps 5C. With straight water cooling that is a huge gain. I don't see how the same would not apply to the A64 unless they are using a synthetic diamond IHS.
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Unread 11-26-2003, 07:03 AM   #208
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Isn't it possible to make some sort of shim to put around the A64core after you've taken the IHS off?
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Unread 11-26-2003, 08:42 AM   #209
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Quote:
Originally posted by nikhsub1
Somehow I highly doubt that. Maybe, maybe when using phase change the differences would be minimal but from my experience with the P4, removing the IHS improved temps 5C. With straight water cooling that is a huge gain. I don't see how the same would not apply to the A64 unless they are using a synthetic diamond IHS.
Could be a fluke or maybe the seating wasn't quite even, but that is what my tests implied. At first it looked like a 7 degree drop, but after further testing with more force on the IHS, it didn't seem to make much difference. Not a scientific test though, so you may be right. The chip is just too expensive to take the risk for a few degrees.
If it wasn't so fragile, I'd remove the IHS again anyway.
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Unread 11-26-2003, 08:43 AM   #210
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Not to be outdone, I hear D-tek has a new block in the works.
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Unread 11-26-2003, 11:41 AM   #211
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Doesn't look like D-Tek has anything to worry about.


Interesting. http://www.overclockers.com/articles373/wbsum.asp

http://www.overclockers.com/articles886/

Takes a 600GPH pump to make this block work as well as a MC5002 with a much smaller pump?

But Player0 has it up there with the Cascade?

Yeah, scientific testing isn't needed.
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Unread 11-26-2003, 11:49 AM   #212
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may not be the 'last word', some discussion on-going
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Unread 11-26-2003, 12:04 PM   #213
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Quote:
Originally posted by unregistered
may not be the 'last word', some discussion on-going
Discussion on? :shrug:
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Unread 11-26-2003, 12:21 PM   #214
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I wish Joe would have tested out all of the nozzles and with the same pump in all cases. His 1.0GPM starting flow point is in a spot where most waterblock C/W curves are in their "knee" and so a small difference in final flow rate can have a fairly big impact on the C/W. If the RBX only moved say 0.6-0.7 GPM with with the 1048 then it might perform a lot worse.

Player0 used the insocket thermistor from an abit motherboard for CPU temps. Temperature compression is not just something I complain about to be a dick...
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Unread 11-26-2003, 12:28 PM   #215
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And keep in mind JoeC tested with the LEAST restrictive inlet insert!

FWIW I have one of the RBXs being sent to me from Cooltechnica today, and nikhsub1 has offered to send a Cascade, an original LRWW, and a DTek WW for as long as I need to test. I calibrated CPU last night and will finish plumbing the test loop and mount the Swiftech MC5000A tonight so that I can start testing it tomorrow. So look for activity to increase around this site a fair amount.

Oh and I went back on coffee since I am staying up all night running tests for you guys. My prostrate says hi!
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Unread 11-26-2003, 01:38 PM   #216
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pH, very glad to see you are going to test the RBX.

JoeC's data is better than others, but I'll trust yours more.

Will you test all 4 blocks?
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Unread 11-26-2003, 01:40 PM   #217
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Will be testing all these blocks and more. I will post one review a week as that gives me a "5 days on; 2 days off" cycle for reviews and 5 reps per block.
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Unread 11-26-2003, 02:04 PM   #218
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The C/W on all 4 of those blocks on the above link on overclockers.com were lower than the Bill test of the WW shown on the site. What's up with that?
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Unread 11-26-2003, 02:08 PM   #219
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Quote:
Originally posted by xgman
The C/W on all 4 of those blocks on the above link on overclockers.com were lower than the Bill test of the WW shown on the site. What's up with that?
Do we have to go over this again? Did JoeC use Bills test bench? No... So the numbers are not going to be the same.

You can search on why as it has been covered many times already.
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Unread 11-26-2003, 02:15 PM   #220
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Quote:
Originally posted by pHaestus


Oh and I went back on coffee since I am staying up all night running tests for you guys. My prostrate says hi!
Needless to say I appreciate it, and all the other stuff you have been doing lately. I would have given up on ProCooling a long time ago if it wasn't for your work. Tired of all these wannabe tech sites more interested in quantity than quality.
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Unread 11-26-2003, 03:22 PM   #221
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Quote:
Originally posted by pHaestus
...and nikhsub1 has offered to send a Cascade, an original LRWW, and a DTek WW for as long as I need to test....
pHaestus, Danny is sending me a D-Tek WW today so I should have it Friday (28th) and I will be sending you all 3 blocks Monday (1st).
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Unread 11-26-2003, 08:15 PM   #222
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Quote:
Originally posted by pHaestus
And keep in mind JoeC tested with the LEAST restrictive inlet insert!

FWIW I have one of the RBXs being sent to me from Cooltechnica today, and nikhsub1 has offered to send a Cascade, an original LRWW, and a DTek WW for as long as I need to test. I calibrated CPU last night and will finish plumbing the test loop and mount the Swiftech MC5000A tonight so that I can start testing it tomorrow. So look for activity to increase around this site a fair amount.

Oh and I went back on coffee since I am staying up all night running tests for you guys. My prostrate says hi!

WOOHOO!
Rock it on!

I will check this often to see whats going on, finally we will all know who's the best WB!
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